Well she is back together and running even better than before. Also, I am now much more familiar with CVK40 carb than I ever thought I would be. I am a bit embarrassed to admit that I worked about 20 hours on the doggone thing, but I did. I wish I had taken notes.
For those who will struggle with their carbed Vulcan 1500s in the future, here is a summary of what I did and why I did it.
After owning the bike about a week, I took the carb apart to see what size my jets were. There was a 170 main, a stock needle with 4 shims and a 45 pilot. The pilot screw was open 1/2 turn.
I re-assembled the carb with 2 shims and the pilot screw opened to 2 1/2 turns. The bike ran but was very rich now as evidenced by the black smoke, and would not run above idle.
My carb had the coolant lines connected to it that made the the already difficult to access pilot screw even more difficult to access. To adjust it meant removing the tank and and pulling the carb off of the intake manifold. This was time consuming as I tried the mixture screw in different positions. None made any difference.
I then tried the carb without the 2 shims on the needle. Same result, way too rich.
Adjusted float. Zero shims on needle. Idle good now, and no more black smoke. However, any attempt to rev above idle cause the carb to backfire. According to articles I have read this is due to a lean mixture caused by the pilot being too small or adjusted too lean. I turned the screw 4 turns out, but there was no change. Time to call it a day.
Day 2:
Went to the Harley dealer and bought a #48 pilot. I would have got a 50 as well, but alas, they didn't have one. Everything I had read to this point indicated that this bigger pilot jet should help or totally fix my problem.
Double checked float height, set at 15mm. Removed and plugged carb coolant lines...I live in the desert for crying out loud.
Though it still wasn't easy, with the coolant lines gone I could now reach the pilot screw without removing the carb from the intake. I broke a screwdriver in order to make it short enough to fit under the carb.
Installed #48 jet, rechecked float, opened screw 2 turns. Re-installed fuel tank, re connect fuel lines..bla bla....
*&^%&!!!!!! Same thing, no change, idle is good but carb popping loud when throttle is blipped. I opened the mixture screw up 4 turns. No difference.
Now I am wondering, is the pilot circuit clogged? If it is, how is it idling? Is it possible for the bike to idle with a plugged pilot circuit?
I forgot to mention that I also drilled the slide with a 1/8 drill and took a scotch pad to the slide just enough to shine it up.
I was back to square one. I placed 3 shims on the needle, and set the mixture screw to 1 1/2 turns out. VROOOOM! No carb popping, no black smoke. Throttle response was definitely improved. I let her idle for about 10 minutes to check for leaks and went for a test drive.
The low end is dramatically better, it's hard to describe accurately but it feels like I picked up a good bit of torque. I'll need to get on out on the interstate in the daytime to find out if the top end has changed.
This was a big pain but the education and the performance gain was worth the hassle. At this point I wonder if the pilot circuit is clogged or not. I also wonder if I really need a # 50 or even bigger pilot. That would seem out of line compared to other 1500s but who knows? I am also curious about what the mileage will be.
For now, I'll leave her alone. I'll order a rebuild kit and some more jets. Now that I've got some experience with this carb, getting the jets dialed in won't be such a daunting task.